
Muncie Dragway, Muncie Indiana (July 30-
Almost UMDRA.com Race #2
Saturday, July 31, 2010 -
Our report is a little late due to computer issues -
In a nutshell -
(1) The spark plug Eric McK picked up for us Saturday morning worked like a charm in the generator!
(2) While Eric was picking up parts for his car and a spark plug for us on Saturday morning, we were searching for and found a local service garage to replace a front wheel bearing on our truck. The truck brought home a souvenir on the front passenger side but, hey, they didn't charge us for the wheel bearing replacement!
(3) Got back to the track 3 hours later to find out the race had been canceled (see pics).
(4) Had a safe trip home on Saturday afternoon. Construction was on the opposite side of the road both to and from Muncie. We saw Michigan's oil spill cleanup, stopped in at Turkeyville for dinner (Finally! Shelly's first time, Bob's second), and were home by 6:30 PM. So, we got a good night's sleep and got up bright and early on Sunday morning and went racing at our home track..




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US131 Motorsports Park, Martin MI (July 9 -
MMPSA.org Thunder Nationals
Friday, July 9, 2010 -
A day with a bike ride is always a good day; except when your cruising down the highway and you feel you cell phone hit your thigh and then slowly skid behind you. So if you are around southbound US131 near the 58th mile marker, look for my LG phone (I could use some of the info on it!)
On a more interesting note... Right as I pull into the track, the Mountain Motor
Pro Stock Association was holding they first qualifying session. Little did I know
that by the time the
weekend ended, I would be quite sick of hearing the PA guy say
“”Mountain Motor Pro Stock”. I made my way around the back of the track and up to
where Bob and Max had parked. We were on the highway side just on the other side
of the fence from the track, about an 1/8th mile past the finish line. It was a fun
place to be parked because every time the Pro Stock guys came down the track the
large boom of them throwing out their parachutes came right in from of us. Plus,
later on Saturday, a nice western breeze brought the nitro from a couple A/Fuel dragsters
would float by our noses!
By the time I had got there Bob and Max had already made a tuning run. The focal point of the day was to play with some clutch converter settings and this run seemed to be half and half. The early numbers were pretty good and the down track numbers were not so great. Just to make sure we got the correct info off that run, we ran it again and got quite similar numbers. For the next two runs we did some more changes trying to find where our limits were. Thinking we found them, Bob put in what we thought was the best of both world (Off the line and down track numbers) and we headed up after the 3rd session of Pro Stock to find we were all alone and everyone was headed home. So we towed back and packed everything into the trailer and hit the showers.
Saturday, July 10, 2010
An early morning came because the gates were lined up so far that they decided
to open them early. The car count for the day was very high. Over 100 in both Modified
and our class: Top ET. They ran two whole sessions of our bracket series before going
into Pro Stock and Alcohol Dragsters. We got our first run in just after 10 AM before
the heat could come and
before all of the humidity could burn off. As we figured
it was a little slow as it always in the beginning of the day not including the added
humidity from the early morning. As the car counts were up, it took almost two and
a half hours to get back around to Top ET so it was well after noon before our second
run. This time our 60ft time came around as well as our down track numbers and ended
up with a 9.32 at 138.5 MPH. Surprisingly, first round came quickly even though Pro
Stock had their last qualifying session. We got everything together when they called
our class as always but somehow we got stuck all the way to the back. Which I guess
came out well, as the dragster we were up against could not make it to the starting
line, we ended up with a competition single. Bob ran a 9.30 on our 9.32 dial sending
us into round 2. There was another few hours and first round of PS and A/F cars before
2nd round. This time we were up towards the front and ready for this round. With
our 9.30 in the first round, we slapped a 9.30 on the side and went up to the line.
After a great .022 light and running just off our dial with a 9.32, the win light
still didn’t come on. There wasn’t much left on the table for the left lane to take
but somehow he did.
I ended up leaving shortly after our lose, before all of the fun went on. Bob and Max stuck around as some of Max’s friends from Chassis Shop were there to make some Nostalgia Funny Car runs in the evening. I had to get back to try and straighten out my phone. Plus, my anniversary is tomorrow so I should probably be around for that.
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Mid Michigan Motorplex, Stanton MI (June 12, 2010)
Looking for that wally!
Saturday, June 12, 2010 -
Yesterday was the National Dragster Challenge (race for a Wally!) at Mid-
The forecast was predicting same hot and humid weather as we had in KY last weekend.
Since we didn't change anything on the bike since KY, it should be pretty easy to
get a good comparison of bike's performance between KY elevation and our home track
elevation.
We thought the gates opened at noon, so we got to the track about 12:30
to discover there was no one in line because we were 2 hours early. Luckily the gate
was open so we pulled in and had plenty of time to eat lunch before the start of
time trials. When we got to the track, we discovered the weather was warm but nowhere
near as humid as KY. There was a steady cooler (head) breeze which helped keep things
cool but dragged down the top end numbers for the bike. By the last round of time
trials, the skies were pretty much clear with clouds to the south and north.
Round
1 -
Round 2 -
Round 3 -
Round 4 -
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